It’s always the same, you think you can do things fast but in the end it takes forever. I’m sure you know this feeling .
First I had to shorten the 30mm shafts
After cutting several shafts with the dremel I found a better technique this time for getting straight cuts. The bell inside a bag is much easier to work with instead of the whole motor with wires. Also you can rotate the bell if you got askew and get a new chance.
On the left side you can see the slice is askew but on the motor side perfectly straight.
After grinding the edges I dremeled a (ugly) flatspot for the grub screw of the helical.
Shaft length check succeeded
Sanding the shafts and inside the helical with 80 grit sandpaper
Time for gluing
The clamps are perfect for holding the motor without any axial backlash (both motors had between 0.5 and 1mm). If you have backlash the motors will rattle badly on every bump or offroad and move left and right when accelerating/braking because of the side load of helicals.
Marked the flat spot for easy positioning of the threaded hole for the grub screw.
Then glued them with Loctite 638 and pressed them hard against the washers for some minutes. This way there is no chance for any gap and the gear sits straight on the shaft. If I would use the grub screw now this wouldn’t be the case.
It’s done, after 24 hours cure time I’ll add the grub screws with Loctite 243 and let it cure for another 48 hours.
I was thinking about a solution for precise mounting of the motor mount and went with ABS sheets between mount and wheel helical.
In the end I used the 2mm ABS sheet plus 0.5mm shrink tube to get the perfect spacing when the helical has 28mm distance to the motor.
This is very covinient for the future. When I change motors it’s always 28mm distance. When I kill the rear truck I buy a new and use the ABS sheet and heat shrink for mounting the drive train.
On my regular MTB I had to re-mount the drives several times because of killed trucks. It’s not fun to find the correct position on the hanger with mounted motor and glued helical. Next is to use the same technique with ABS sheet spacer there, too. Very soon I can do it because I’ve bent the 12mm solid axle and actually waiting for a new rear hanger.
And this is the max. tilt before the motor would hit the deck, that should be enough.
Have a nice day